Great to see they've pushed out an update quickly.
Flew today with the 1.1.4 update. These are my findings:
Dunno what they mean by slew control, it is still disabled.
A new bug seems to have been introduced. I flew for about 3 minutes then the gimbal went haywire. I landed quickly. The light had gone blue...like the USB was connected...and the tilt servo was rotating continuously having undone the tray screw. So it seems the "cutoff when there is something wrong" feature doesnt work either.
Also I dont know whether it is a new thing or not. My pan control servo is independent of the RSGS because pan has not been implemented yet, although it is advertised on the PH site. When I pan the gimbal, the tilt and roll servos start glitching, ruining the video.
I am powering the servos via the Pan input, This is because if the rx powers the servos, they glitch all the time and powering them this way seems to cure it to a certain extent, but only at very low gain values (one division off zero, or 10%) Any higher than this I get glitching.
The trouble with this is, at this low gain setting. the gimbal does not correct quickly enough and the video does not stabilise. Higher gain is needed but higher gain introduces glitching and judder.
I dont think the RSGS is there yet. Mine is certainly not "Rock Solid". It looks like I am going to have to put the pots back on and stabilise in the traditional way until this unit is sorted.
I agree with the comments about lack of guidance. I can usually work things out without a manual, but only if the device is not too quirky.