ichwillnix
Member
Sandor the board did not work ever since i got it with the original connector before i cut it off.
No throttle response from any of the motor outputs. LED's and beeps yes but no throttle.
After i chopped off the connector ( i think it may have been 1 or 2 days later) and soldered the wires inside the two bullet female like parts still soldered to the boards, same thing, LED's came on as before, beeps but no throttle response just as before.
So there was no difference in the behavior of the board.
I made a second mistake after desoldering to wires by cleaning the inside of the female bullet like connectors just prior tp packing it and shipping it which might account for the copper dust.
Anyway here and now i ask you to try the board.
Power it up and see if you get the blue LED's to come on and a beep or more from a motor connected to any of the outputs.
If there is than it is the same board that i received before i cut off anything.
If it goes up in smoke than it is my fault entirely, i screwed up the board and will apologise to you and everyone else i troubled here and elsewhere.
But if the board does respond by turning on the LED's and the outputs with a motor connected behave just as they did like they did the very same i unpacked it and tried it, then what?
I would not try to blame my mistakes on any one.
I take responsability for my deeds.
If i broke the board, i will send you the 450$ i still have to my name as reparations and i apologise to you.
But if i didn't break anything, except that i removed the original connector and in the process touched and put some marks on the bullet females on the sides will you fix it and show proof here on the forum that it works before you ship it back to me?
Hello guys!
I have to apologize at all for drawing a too fast conclusion and blaming Sandor without having the real board in my hands and finding the rootcause for it.
I think the mistakes done here are distributed on all of us.
@ Victor:
Without having the board in my hands yet (i will receive it soon) and only by listening to your descriptions i believe that the board is still working and is also correctly programmend. The LEDs are only blinking and the motors are only "beeping" when the have
a) the correct firmware installed
b) the connections (motor, PPM-signal and battery supply) are done correctly
c) the Herkules ESCs receive a valid PPM signal.
When the Herkules is beeping and blinking, we have 95% of the job done. The only thing i could imagine is that the PPM-Signal doesnt reach safely 0% (means less than 1.1msec Pulse with). The Herkules has a lock mechanism which prevents the motor from starting when power supply is applied with a throttle value higher than 20%). This avoids the motors from spinning up uncontrolled when the battery is connected. Maybe you should check your signal source. Do you use a servo-tester or the wookong system? Did you calibrate the ESC with the wookong? I don't know the DJI in detailed but i have something in mind that has to be done.
By the way, we are currently building our own Oktokopter with DJI and 2x Herkules Boards and we will do intensive tests and then we will place also a detailed description (manual) with do's and dont's on our webpage.
As i told, this is only an assumption. I will check this in detail when i have the board. Victor, i promise you that you will receive soon a fully working board and we will bring your copter airborne. I will send it to Sandor and he will ship it to you.
Remark 1: The sawing copper dust on the pictures are not good for the electronics. As sandor told, you make shorcuts on a lot of the fine-pitched pins. It will be difficult for us to clean it from all that dangerous dust...
Remark 2: Victor, it is not a good thing to post private email communication with company infos to a public forum. Please never do this again! This does not improve communication lacks!
@ Sandor:
Again sorry for blaming you so quickly. I trust in you that you delivered the board 100% fully working. Nevertheless we have to work together and find solutions to make it as easy as possible for Herkules users to implement the ESC easily without any stress and helping them to bring the copter safely and fast to the air.
We are thinking of providing a "ready to use" ESC by default (maybe boxed) with only connectors for motors, battery and signals with no need of soldering at all.
This helps really all customers who want to spent more time with flying than with building and soldering.
@ Me:
I will still try to provide good support to all of the customers as good as i can. In future i will firstly analyze the problems personally and then drawing the conclusions.
Sorry again for all guys i judged about and i apologize again.
=> Lets concentrate now again on the good technical work and bringing more Copter airborne....
Andreas