98 Snake Eater
Member
Some info on my setup:
DJI F550 frame
NAZA M (original)
GPS
30Amp ESC's (model unknown, but heat shrink has Turnigy printed on it)
RcTimer 2830/14 750kv motors
4s 5000mAh Lipo
AR8000 Rx
DX6i Tx
Apart from the recently upgraded receiver, I've been flying this setup for over a year without much issue.
It has always been smooth, stable and held position like a rock.
However, it recently developed a problem with twitchy controls, scary stability and random changes in altitude :upset:
Here's a video from a few weeks ago where she was flying as she should:
www.youtube.com/watch?v=6_04BvGmbcg
Fast Forward to about ~3:40 and you'll see she holds solid in GPS mode even in high wind.
I then switch to ATT mode, she drifts with the wind, but holds altitude just as she has from day one.
Now here's a video from yesterday:
www.youtube.com/watch?v=qgTBVTZH2DA
As you can see, she drifts all over the place in either GPS or ATT mode.
The sticks are twitchy and the altitude randomly changes even with center sticks.
So far, I've tried the following:
1) Re-Calibrated Tx Controls
2) Re-Calibrated GPS Compass
3) Re-Calibrated IMU
4) Re-Positioned Rx away from the NAZA USB doohicky
5) Covered the sides of the NAZA with electrical tape
6) Held frame down as I powered up to full throttle and moved the right stick in all positions to check motors, blowing crap all over my office
7) Checked all motor wires and wires leading into the NAZA
I have a feeling the internal barometer in the FC is fubar'd, but I'm open to suggestions at this point
DJI F550 frame
NAZA M (original)
GPS
30Amp ESC's (model unknown, but heat shrink has Turnigy printed on it)
RcTimer 2830/14 750kv motors
4s 5000mAh Lipo
AR8000 Rx
DX6i Tx
Apart from the recently upgraded receiver, I've been flying this setup for over a year without much issue.
It has always been smooth, stable and held position like a rock.
However, it recently developed a problem with twitchy controls, scary stability and random changes in altitude :upset:
Here's a video from a few weeks ago where she was flying as she should:
www.youtube.com/watch?v=6_04BvGmbcg
Fast Forward to about ~3:40 and you'll see she holds solid in GPS mode even in high wind.
I then switch to ATT mode, she drifts with the wind, but holds altitude just as she has from day one.
Now here's a video from yesterday:
www.youtube.com/watch?v=qgTBVTZH2DA
As you can see, she drifts all over the place in either GPS or ATT mode.
The sticks are twitchy and the altitude randomly changes even with center sticks.
So far, I've tried the following:
1) Re-Calibrated Tx Controls
2) Re-Calibrated GPS Compass
3) Re-Calibrated IMU
4) Re-Positioned Rx away from the NAZA USB doohicky
5) Covered the sides of the NAZA with electrical tape
6) Held frame down as I powered up to full throttle and moved the right stick in all positions to check motors, blowing crap all over my office
7) Checked all motor wires and wires leading into the NAZA
I have a feeling the internal barometer in the FC is fubar'd, but I'm open to suggestions at this point