Carcara
Member
Hello all,
I recently put together a new distribution board with 4 new BLCtrls 2.0, this is the setup:
Mikrokopter Flight Ctrl Board HW V2.0 / SW V2.08a
Mikrokopter Navi Ctrl Board HW V1.1 / SW V2.08a
MK3 Mag V0.23a
BL Ctrl V0.31
Axi 2820/14 motors
APC 14 x 4.7 slow flyers
Quadro X configuration
On all of my flights I get these strange current readings for motors 2 and 3, where they show much more current consumption compared to the other 2 motors. I know it´s not the motors that are causing the problem, because after swaping motor 1 and 2, the higher reading continues on motor 2 position. The weird thing is that the temperature after flight are all the same, regardless of motors 1 through 4.
I can send the last flight log file so you can take a closer look (could not upload a .gpx file at this post!)
Any help is appreciated.
Regards,
Marcelo.
Flight date: 20/02/2015 15:07:21
Flight time: 15:07:21.8 - 15:08:17.2 (55 secs, 00:00:55)
Batt. time : 60 secs, 00:01:00
Start Location : -30.0851704 / -51.0576908 @105,9m
Elevation(GPS) : 0 42,96 389,4 m (min/avg/max)
GPS alt. (raw) : 104,375 127 389,4 m
Altitude(Barom.): 0,5 5,12 9,8 m
Vertical speed : -0,76 0,11 0,74 m/s
Max speed : 10,1 km/h
Max target dist.: 0 m
Max distance/LOS: 228,7 m / 228,7 m
Sats : 0 5 7
Voltage : min. 14,3, max. 14,9 V
Current : 0,5 18 27,3 A
Wattage : 7 278 393,12 W
Capacity: 317 mAh
Motor1: 0,0 2,9 4,4 A Temp: 34 56 69 °C
Motor2: 0,1 6,0 9,0 A Temp: 32 51 62 °C
Motor3: 0,0 6,3 9,0 A Temp: 33 53 65 °C
Motor4: 0,0 2,5 4,3 A Temp: 35 51 61 °C
Magnet Field: 96 114 125 % (!)
Magnet Inclination: 46 48 55 deg
No errors found
I recently put together a new distribution board with 4 new BLCtrls 2.0, this is the setup:
Mikrokopter Flight Ctrl Board HW V2.0 / SW V2.08a
Mikrokopter Navi Ctrl Board HW V1.1 / SW V2.08a
MK3 Mag V0.23a
BL Ctrl V0.31
Axi 2820/14 motors
APC 14 x 4.7 slow flyers
Quadro X configuration
On all of my flights I get these strange current readings for motors 2 and 3, where they show much more current consumption compared to the other 2 motors. I know it´s not the motors that are causing the problem, because after swaping motor 1 and 2, the higher reading continues on motor 2 position. The weird thing is that the temperature after flight are all the same, regardless of motors 1 through 4.
I can send the last flight log file so you can take a closer look (could not upload a .gpx file at this post!)
Any help is appreciated.
Regards,
Marcelo.
Flight date: 20/02/2015 15:07:21
Flight time: 15:07:21.8 - 15:08:17.2 (55 secs, 00:00:55)
Batt. time : 60 secs, 00:01:00
Start Location : -30.0851704 / -51.0576908 @105,9m
Elevation(GPS) : 0 42,96 389,4 m (min/avg/max)
GPS alt. (raw) : 104,375 127 389,4 m
Altitude(Barom.): 0,5 5,12 9,8 m
Vertical speed : -0,76 0,11 0,74 m/s
Max speed : 10,1 km/h
Max target dist.: 0 m
Max distance/LOS: 228,7 m / 228,7 m
Sats : 0 5 7
Voltage : min. 14,3, max. 14,9 V
Current : 0,5 18 27,3 A
Wattage : 7 278 393,12 W
Capacity: 317 mAh
Motor1: 0,0 2,9 4,4 A Temp: 34 56 69 °C
Motor2: 0,1 6,0 9,0 A Temp: 32 51 62 °C
Motor3: 0,0 6,3 9,0 A Temp: 33 53 65 °C
Motor4: 0,0 2,5 4,3 A Temp: 35 51 61 °C
Magnet Field: 96 114 125 % (!)
Magnet Inclination: 46 48 55 deg
No errors found