brind0g
Member
As the title suggests, I tried to fly my quad for the first time since building it today. I noticed a few things and need some advice/guidance as I am still very new to the scene.
First thing I am not sure about is after doing a factory reset on the KK2 board im using, the elevator control seems to be reversed, so when i push the stick forward, it shows as "back" on the KK2 board LCD.
I also have an issue with the motors powering up at different speeds. They seem to come on together, but even when i just put throttle on 10 - 20%, one Motor1 just keep increasing in speed. Motor 4 hardly spins, if at all.
Is there are particular order I should reset everything?
I am using Turnigy Plush 25A escs, which I have programmed with the programming card.
I have checked motor orientation and props are the correct direction for each motor.
My Tx is a Spektrum dx7s
I am going to try suspending the quad tonight and see what I can find with the auto leveling etc.
Thanks in advance
First thing I am not sure about is after doing a factory reset on the KK2 board im using, the elevator control seems to be reversed, so when i push the stick forward, it shows as "back" on the KK2 board LCD.
I also have an issue with the motors powering up at different speeds. They seem to come on together, but even when i just put throttle on 10 - 20%, one Motor1 just keep increasing in speed. Motor 4 hardly spins, if at all.
Is there are particular order I should reset everything?
I am using Turnigy Plush 25A escs, which I have programmed with the programming card.
I have checked motor orientation and props are the correct direction for each motor.
My Tx is a Spektrum dx7s
I am going to try suspending the quad tonight and see what I can find with the auto leveling etc.
Thanks in advance