traxx2003
Member
Hello everyone! First allow me to offer some details of my build and some details of the problem I'm having:
Skyhero 850 X4 configuration
TMotor 4120 400kv
KDE 55AESC's
SuperX controller
17x5.5 CF props
EZUHF control system
My problem:
I first attempted to use a Pixhawk FC with this build but after experiencing some issues with compass calibration errors I've decided to try a SuperX controller I already had. Below are some ofvthecisdues I'm axperiencing:
- With both the Pixhawk & SuperX, the motors just sound like they are running at too low RPM. Tge hover is just not stable, the quad has a tendency to drift toward the right/rear (more pronounced to be just ATTI normal drift).
-After countless attempts to get the gains dialed in with both FC's this think will not hover in a stable manner. CG is spot on and in line with FC.
- With Pixhawk I noticed that both motors &ECS's ram much cooler after a 10 minute autotune / hover test flight. Motors & ESC's were 42 degrees C after a 10-15 min hover flight. With the SuperX the ESC's were super hot, could not keep finger on them for more than 2 sec.
My theory is since I'm experiencing somewhat similar problems with two different FC's I could be dealing with faulty motors or ESC's?
How could I troubleshoot a potentially faulty motor or ESC? Not sure what to do.
Skyhero 850 X4 configuration
TMotor 4120 400kv
KDE 55AESC's
SuperX controller
17x5.5 CF props
EZUHF control system
My problem:
I first attempted to use a Pixhawk FC with this build but after experiencing some issues with compass calibration errors I've decided to try a SuperX controller I already had. Below are some ofvthecisdues I'm axperiencing:
- With both the Pixhawk & SuperX, the motors just sound like they are running at too low RPM. Tge hover is just not stable, the quad has a tendency to drift toward the right/rear (more pronounced to be just ATTI normal drift).
-After countless attempts to get the gains dialed in with both FC's this think will not hover in a stable manner. CG is spot on and in line with FC.
- With Pixhawk I noticed that both motors &ECS's ram much cooler after a 10 minute autotune / hover test flight. Motors & ESC's were 42 degrees C after a 10-15 min hover flight. With the SuperX the ESC's were super hot, could not keep finger on them for more than 2 sec.
My theory is since I'm experiencing somewhat similar problems with two different FC's I could be dealing with faulty motors or ESC's?
How could I troubleshoot a potentially faulty motor or ESC? Not sure what to do.