Hello, i have a big quad (1,5m of diameter and weight about 20 Kg) for professional use with Hoverfly Pro, Hoverfly Gps, Castle Creations Ice2 HV 120, 4 motors AXI 5320/18 and Spectrum Dx8 Radio, 4 batteries 5,3 Amps 22,2V.
Some time ago we were flying and shoot for a film and suddenly, while we were returning to land, quad seemed to descend too fast, so we give more throttle but... nothing.. the motor speed not changed but remain at half throttle speed... after quad go down and broke 1 arm.
We repaired quad and the day after all was ok, we made 1 day of shoot and quad was fine.
After 1 week, we was testing new camera head settings and, after 5 flight fine, seem problem, the throttle did not increase motors speed and quad made another crash.
So we decide to change radio and receiver with another Spektrum Dx8, 1° flight all ok, second flight, same problem and other crash.
Today, after 2 flight same problem another time.
Battery after crash are ok, remained 60% power.
So throttle not work over 1/2 position some times, the motors speed remain about ad half power (fortunately does not go to 0) , all other commands are ok, only throttle was problem
I have last firmware, every time with crash we have flight with AL inserted, without GPS (switch of GPS to off).
I have checked all settings with Hoverfly tool, throttle endpoints are ok, the cursor on Tool go from 0 to max (not go to middle with max value), all switch are ok, all work correctly,.
I check also Castle Creations logs and i saw that the throttle before all crashes is not increased, it's remained constant.
The problem is extemporaneous and for us is impossible to work in this situation.
Here is a video of crash from quad, from audio you can hear that motors did not increase the speed, but when quad become to descent the throttle stick was to max value..
http://www.youtube.com/watch?v=XTFjysX2M7A&feature=youtu.be
Have you any suggest?
Thanks
Marco from Italy
Some time ago we were flying and shoot for a film and suddenly, while we were returning to land, quad seemed to descend too fast, so we give more throttle but... nothing.. the motor speed not changed but remain at half throttle speed... after quad go down and broke 1 arm.
We repaired quad and the day after all was ok, we made 1 day of shoot and quad was fine.
After 1 week, we was testing new camera head settings and, after 5 flight fine, seem problem, the throttle did not increase motors speed and quad made another crash.
So we decide to change radio and receiver with another Spektrum Dx8, 1° flight all ok, second flight, same problem and other crash.
Today, after 2 flight same problem another time.
Battery after crash are ok, remained 60% power.
So throttle not work over 1/2 position some times, the motors speed remain about ad half power (fortunately does not go to 0) , all other commands are ok, only throttle was problem
I have last firmware, every time with crash we have flight with AL inserted, without GPS (switch of GPS to off).
I have checked all settings with Hoverfly tool, throttle endpoints are ok, the cursor on Tool go from 0 to max (not go to middle with max value), all switch are ok, all work correctly,.
I check also Castle Creations logs and i saw that the throttle before all crashes is not increased, it's remained constant.
The problem is extemporaneous and for us is impossible to work in this situation.
Here is a video of crash from quad, from audio you can hear that motors did not increase the speed, but when quad become to descent the throttle stick was to max value..
http://www.youtube.com/watch?v=XTFjysX2M7A&feature=youtu.be
Have you any suggest?
Thanks
Marco from Italy