I installed the Naza GPS module on my FlameWheel F450 today. After calibrating it, I tested out the RTH feature and had the following experience: after hovering the quad about 6 ft off the ground and about 15' from the launch position, I activated the Go Home Landing failsafe. The copter rose to about 60', which I was expecting, and then it started circling the home position area. It circled about 3-4 times but it didn't look like it was descending so I switched it back to GPS Attitude mode and landed it manually.
On the second test flight, I flew the FW about 40 yards away from the launch site and turned on the failsafe. This time the quad flew to within a 3-4 feet of the home position and hovered about a foot off the ground. When it tried to land, it hopped once, and one of its legs got caught in the grass so it flipped over.
Tomorrow I am going to test the RTH feature again. I think on the first flight I didn't wait long enough for the home position to be locked by the GPS even though I didn't take off until I got a blinking green light on the VU. On both test flights I didn't turn the Tx off, but I think I will try that tomorrow.
If anyone has any comments or ideas about what happened on my tests today I would appreciate any feedback and suggestions for improving my setup.
Here is what I am flying:
FlameWheel F450
Naza V1 with 3.14 firmware
DJI 30A ESCs
RCTiger 770kv motors
APC 10 x 4.7 props
DJI Naza GPS module
V2 PMU
4500 mAh / 4S / 14.8v / 30C batteries
Spektrum DX8 radio
Spektrum AR8000 Rx with Telemetry
Flight Modes: GPS, Attitude, RTH failsafe
No IOC
Gains: 120, 120, 120, 120, 80, 80
On the second test flight, I flew the FW about 40 yards away from the launch site and turned on the failsafe. This time the quad flew to within a 3-4 feet of the home position and hovered about a foot off the ground. When it tried to land, it hopped once, and one of its legs got caught in the grass so it flipped over.
Tomorrow I am going to test the RTH feature again. I think on the first flight I didn't wait long enough for the home position to be locked by the GPS even though I didn't take off until I got a blinking green light on the VU. On both test flights I didn't turn the Tx off, but I think I will try that tomorrow.
If anyone has any comments or ideas about what happened on my tests today I would appreciate any feedback and suggestions for improving my setup.
Here is what I am flying:
FlameWheel F450
Naza V1 with 3.14 firmware
DJI 30A ESCs
RCTiger 770kv motors
APC 10 x 4.7 props
DJI Naza GPS module
V2 PMU
4500 mAh / 4S / 14.8v / 30C batteries
Spektrum DX8 radio
Spektrum AR8000 Rx with Telemetry
Flight Modes: GPS, Attitude, RTH failsafe
No IOC
Gains: 120, 120, 120, 120, 80, 80